Call to getBright() hangs forever.

Bug #804298 reported by Victor Norman
14
This bug affects 3 people
Affects Status Importance Assigned to Milestone
Myro-C++
Invalid
Undecided
Unassigned

Bug Description

This simple code makes my program hang.:

connect();
cout << robot.getBright("right") << endl;
disconnect();

I have Ubuntu 10.04, Scribbler2, fluke 2.9.1, scribbler firmware 1.0.2, myroC++ 2.2.2.

Revision history for this message
John Hoare (jhoare) wrote :

I am unable to replicate this on my setup, using a Scribbler 1. Unfortunately, I do not have access to a Scribbler2 to test it.

Changed in myro-c++:
status: New → In Progress
Revision history for this message
John Hoare (jhoare) wrote :

Can you verify that this always happens? Perhaps this only happens when the scribbler is not correctly connected? Can you verify under the same connection that other functions are working? I'll admit we haven't really used getBright() in any of our labs.

Revision history for this message
John Hoare (jhoare) wrote :

Okay, After implementing the senses() and getAll() functions, i'm getting this behavior as well.

Revision history for this message
John Hoare (jhoare) wrote :

Looks like (verifying with Python Mailing list) this is likely a bug w/ the blueooth stack, of the fluke has gotten into a weird state. When I was having difficulties, it was not working with the Python version either.

Changed in myro-c++:
status: In Progress → Won't Fix
status: Won't Fix → Invalid
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